Hi all...I am at my wits end...never been stumped

83 Mighty max with 4d55....blew head gasket maybe 5 years ago...truck sat in barn till three weeks ago...installed a new 4d56 head recently, bled the fuel lines multiple times, new glow plugs...engine will act like it wants to start but doesn't , hours of cranking..

Specifics:

Valves adjusted cold to .15 just readjusted to .25 ..
Reused 4d55 injectors, snug in hole but are screwed in and no compression leaking.
When glow plugs are pulled, healthy compression shooting out of each hole.
Glow plugs functional and working...blueish tips from heating up.. 5 seconds..
timing has been double checked and is correct on all three indicators

Am noticing a lot of exhaust smelling (not white) smoke coming out of the valves under the valve cover...seems to be throughout the head...lot of smoke...

I'm ready to throw in the towel unless somehow has words of wisdom...